Gerald

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Log from real HW - https://logs.px4.io/plot_app?log=6b1553f3-734b-4800-a286-7f11eed45373 - All 4 motors are spinning. - RC input can not be detected from FrSky R-XSR receiver connected to RC IN.

@davids5 i faced a hardfault after updating the FW. [20221024_RT10602-v2_hardfault.txt](https://github.com/PX4/PX4-Autopilot/files/9849860/20221024_RT10602-v2_hardfault.txt)

Hmm, can't recall But the FMU is rebooting now several times while connected via USB. Unfortunately my debug cable is already in one of the cases for traveling. Therefore i...

> Hmm, can't recall But the FMU is rebooting now several times while connected via USB. Unfortunately my debug cable is already in one of the cases for traveling. Therefore...

i did a clean build again resulting in crash when initializing GPS [fmurt1062-v2_test_20221026.txt](https://github.com/PX4/PX4-Autopilot/files/9866433/fmurt1062-v2_test_20221026.txt) I can not get a console prompt on the debug port. so it seems really stalled.

Hi @davids5 , i had a succesful maiden flight of the fmurt1062 RC03 HW. No tuning, just functional HW test. Unfortunately no logs are written. Therefore just the video ->...

Btw, Ethernet is working. I'm connecting my QGC Laptop via Ethernet at the moment.

First test with RC04 HW and baseboard with T1 ethernet done. Flashing - OK GPS port - OK T1 ethernet port - OK, got IP via DHCP and mavlink connection...

Yes and also Iain is facing this USB issue

When setting the Airframe to "NXP HoverGames" i'm getting this hardfault [20230201_rt1060_hardfault.txt](https://github.com/PX4/PX4-Autopilot/files/10332367/20230201_rt1060_hardfault.txt)